Pilot (slow) Jet needs to be thoroughly cleaned. Gap all 4 plugs to 0.031" (0.8 mm) which is lower end of the Honda spec. And from another similar thread where I wrote this:
Great that you cleaned the carb. Since it sat for so long, gas gone bad could have scunged up your fuel filter screens, clogging them, and causing a lean condition by inhibiting fuel flow. Have you addressed this potential problem? And I can't emphasize enough the use of SeaFoam gas treatment to clean the entire fuel system.
Also, there's a bigger fuel screen inside the tank, attached to the petcock, that could be totally scunged up as well:Our carb inlet fuel screen:
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It's tiny:
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Where it goes:
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The fuel line inlet port:
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#4 in this fiche diagram from partzilla.com:
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Now that I know how to post a video - as a public service announcement - I'd like to post Gonzo1970's YouTube video for the purpose of 'comparison-setting' your idle speed to proper 900 rpm, if you don't have a tachometer. Just play the video/audio on your phone, tablet, or laptop and adjust your Throttle Stop Screw Knob to match the cadence. And many thanks to Gonzo for making/posting that video ~4 years ago on YouTube - it has always been very valuable!
:cheers:
^^^ Above, you should see a YouTube video screen with a red 'play' button, not a hyperlink. If you see a hyperlink, then on your mobile device, select 'full-desktop view' or equivalent - or simply scroll to bottom of this page and select "vB4 Default Style" in the bottom-left pulldown menu in the dark-blue bar across the bottom of the page.
...I'm thinking perhaps it may be the pilot jet because I didn't have a wire small enough to fit through it entirely. It was small enough to clean out the side holes on it, but not the main passage. I did soak it in carb cleaner for over 20 minutes though so I was thinking that should have been plenty of time to break up the junk.
Pilot (slow) Jet needs to be thoroughly cleaned...
You must clean that main passage of the Pilot Jet! I would do that in addition to the steps you list, above. I don't have my pin gauge set available, but on my stocker 55 Pilot Jet it looks like the main passage is approximately the same diameter as the 'side' holes:I don't actually have the gas tank on at all, so it shouldn't be a petcock related issue.
As far as I understood if you bypass the petcock like I am, it shouldn't be any different from using a standard petcock/carb setup?
Also, the battery is brand new and hooked up to a battery tender during the testing.
I did not know about the carb inlet screen. I'm now wondering if it is even on mine at all or if it fell out or something. I'll have to check.
Sounds like I will do the following next (since I don't have any parts off hand. If these don't work then I'll have to go buy some):
- Check carb inlet screen
- Check the spark gaps again
- Check the Throttle Stop Screw Knob with the video to see how it impacts
Anything I'm missing?
Right on, man! :cheers:After seeing your image, I'm thinking that it's definitely a pilot jet issue then. I was thinking the hole was a lot smaller and that's why I wasn't able to push it through but I can't even see through mine like that. Looks like I have the right size but the wire isn't a sturdy enough material to push it through.
When I said I don't have parts I meant I don't have diaphragms or hoses laying around to replace any that I inspect. I will definitely check the hoses and diaphrams.
I'll have to go get something to clean out the jet better. I will keep you guys updated on my progress. Nothing like seeing a thread unresolved or with just "It works now!"
I just found some notes I took when I pin-gauged all the jets I have. At the time, I measured the main (axial) passage of the Keihin 55 Pilot (Slow) Jet (Honda OEM) - which in Keihin and Factory Pro (FP) terms, '55' means 0.55 mm diameter - to be 0.021" (0.533 mm) diameter. It appears that I did not measure the side holes diameter, but at least now you know that you need a wire (or drill bit that small?) of about 0.020" (0.5 mm) to fit through the main passage of a Keihin or FP 55 Pilot Jet to know that it is cleaned out properly.You must clean that main passage of the Pilot Jet! I would do that in addition to the steps you list, above. I don't have my pin gauge set available, but on my stocker 55 Pilot Jet it looks like the main passage is approximately the same diameter as the 'side' holes:
End view of Keihin 55 Pilot Jet:
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Well, alright!! Good idea - nice work, man... glad I could help! :icon_susp :glee: Thanks for reporting back! :mosh:Update: I got it working! (for the most part)
Turns out the pilot jet was about 10x more dirty than I thought.
I ended up buying an 88 cent BBQ brush and pulling a few wires out of it to push them through the pilot jet. I had to soak it in carb cleaner for about 10-15 minutes before I could even get the wires through though. It was super clogged apparently.
Thanks everyone for the ideas/suggestions. I still need to adjust the idle and some other things, but it looks like like my VTX is almost ready to ride!